AR88 Fault Finding
With most equipments I work on there are "stock faults".
These are the faults that occur most frequently.... often being
due to poor circuit design, or defects in the components used.
Sometimes one can see problems because the circuit board has changed
colour from overheating, the component may have burnt or just
gone dead short from internal overdissipation melting a semiconductor
junction. More often than not inadequate soldering has resulted
in dry joints which can arc and destroy semiconductors or burn
switch contacts. Nowadays components seem to be getting physically
smaller and lighter but their specification is no worse than it
used to be. Maybe its because tolerancing has improved or, more
likely pressures of pricing has cut away any vestiges of contingency
in the design? Going back to 1942 things were built differently....seemingly
weight, at least, was no object!
Faced with a hefty AR88 and a blank sheet regarding stock
faults I decided to use inspired guesswork to cure what seemed
to be pretty major faults. What faults? Well the thing seemed
to receive stations on a short length of wire but when I connected
100 feet of the stuff the receiver didn't like it one little bit.
Signals were too powerful and wouldn't change or reduce in strength
when AVC was switched in or out. A howling noise accompanied medium
wave broadcasts and SSB was totally indecipherable. The RF gain
control had absolutely no effect, and with the switch set to either
of the two noise limiter positions the receiver went dead.
I looked at the circuit diagram and found the AVC and adjustable
RF gain circuit. The gain pot is cleverly connected to the HT-
circuit just "north" of two resistors connecting it
to deck. This ensures a solid negative voltage wrt ground which
can be used as a source for biasing back the control grids of
the RF and IF amplifiers. Between the pot wiper and chassis I
measured 30 volts negative to ground which should be plenty to
mute most valves. The centre of the pot connected to a 390kohm
resistor which I measured, with the set off of course. It measured
nearer 3.9Mohms than 390kohms. I removed it and found it was OK
but anyway as it was out I fitted a new resistor but this also
read 3.9Mohms back in circuit. I never understood this as a meter
test at either end to ground and across the resistor revealed
zero volts so I put it down to "the fault". Next I checked
the voltage at the far side of the 390kohm resistor. It was about
minus 2 volts or thereabouts... surely wrong considering all the
trouble to establish minus 30 volts! Now one thing I'd noticed
was that all the old paper decoupling capacitors had been changed
to new plastic types... except those lovely squarish metal Sprague
style cans. Presumably these were OK? I checked the circuit diagram
against the component layout drawing... unlike printed circuits
there are no screen printed markings to go on. Three 0.05uF capacitors
were included in a single can. One for decoupling the AVC line
and the other two in parallel for decoupling the noise limiter
circuit. I unhooked the AGC capacitor and instantly the receiver
gain took a dive. The RF gain control pot was now working! I unhooked
the other pair and suddenly the noise limiter sprung into life.
The two caps in parallel read about 500kohms and the single about
700kohm. New capacitors restored the proper functioning of AVC
and noise limiter.
I looked around and found the audio coupling capacitor was
a nice new 0.1uF plastic type. The circuit said two 4700pF in
parallel. Somebody's maths is a bit suspect? I swapped the 0.1uF
for a new 0.01uF.
As the BFO was a bit timid I looked at the circuit... not
at all clear! In the descriptive part of the manual the BFO is
said to be connected to the rest of the receiver "electrostatically".
It certainly isn't "electrically" as the connection
is via the 6J5's octal socket pin 4. The valve doesn't have a
pin 4.. that must have something to do with the "static"
bit? Anyway I decided not to change things as the old designers
must have known what they were doing. Sideband reception is fine
so long as the RF gain is kept down. One can't readily "zero
beat" AM stations without first cranking down the RF gain
cos there just isn't enough oomph.
For the time being the receiver is working well enough to
screw back its base panel but I must find some really chunky rubber
feet. The flimsy things fitted are now only three in number and
those looking pretty tired having to each accommodate some 35
odd pounds dead weight plus an enormous shear force of some 250
ft.lb as the receiver is pulled across the bench.
Next I tackled the IF tuning. I'd noticed that there was a
strong local station on Medium Waves with a weaker identical signal
next to it. The second signal wasn't supposed to be there; probably
due to false peaking in the IF strip. Initially I checked the
centring of the tuning then swept the IF pass band with an oscillator.
After peaking the coils using the "wobbulated" test
signal the ghost stations had disappeared.
I'd noticed that the two tuning dials seemed to be leaning
over. The centre cursor line for each was about quarter of an
inch to the right of where the dials wanted to show vertical divisions.
As the set had been used as a coffee table, showing rings from
mugs on one end I'd initially accepted the premise that the front
end had somehow settled with the assistance of gravity. However
when I slackened off all the securing screws I found the mating
holes allowed no adjustment. After puzzling for some time I reckoned
that long ago the front panel had been removed and the plastic
scale had been detached. The scale has a number of securing screws
which allow some movement left/right so that it can be lined up
with the centre-lines of the two dials. Unfortunately whoever
assembled the thing hadn't noticed and put it all back together
without checking mechanical alignment. There are twelve securing
screws. Eight are accessible but four are behind the two dials
and this means that the front panel has to be detached before
the scale can be re-located. I looked at the large number of inaccessible
quarter inch bolts and decided that this must remain a task for
another day when I've nothing better to do. In the meantime I
adjusted the position of the cursor lines by sliding their mounting
brackets fully left. Now at least the vertical divisions on the
dials line up with the cursors when vertical although the whole
assembly is shifted to one side.
Firing up the receiver on 40 metre sideband showed sensitivity
and stability was excellent. Frequency accuracy was out by just
less than quarter of an inch because the dial cursor is too far
to one side and anyway over the years electrical adjustments have
drifted a little but I'm loathe to touch the front end alignment
until I'm happy with the mechanical position of the dials.
One interesting fact...Idly tuning the band between 30 and
32 MHz revealed some very strong signals. These turned out to
be from cordless phones. Probably not many people know about these
because very few short-wave or communications receivers go above
30MHz. When sun spots are just right some of these local phone
conversations may bridge the Atlantic and given a suitable narrowband
FM receiver will provide listeners with hours of mystifying information.
Seriously though, after only eavesdropping for a few moments,
I was provided with names, addresses, telephone numbers and I'm
sure if I'd hung around longer, things like credit card information.
Be warned.. as the old posters used to say (and no doubt current
ones on the walls of offices at GCHQ).."Be careful what you
say.... walls have ears!"
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