
This unit was built back in the early seventies
to power a 19" balsa wood model tug which I had been given - a
Titan,
built from a Veron kit. (and later re-named Bluebell after
the brand of of metal polish used so lavishly in the engine room)
The requirement was that it should be
fail-safe, particularly against propellor fouling in our local pond. It
must drive the model at scale speed with power to spare for at least 30
minutes without attention and it must be clean, dry and run cool enough
to avoid damaging a highly finished wooden deck and superstructure.
Fuel would be methylated spirit (alcohol)
and lamp control would allow "Full" or "Half" speeds ahead, under radio
control.
The space available was 9.5" x 3.75" with
3.5" height available for the boiler, dropping to 2.375" under the engine
room hatch and it was decided to build the complete plant as a single unit
which could be lifted from the boat for filling, cleaning etc.
The very restricted height in the engine room led to the
adoption of a Stuart Turner ST 7/16"x7/16" double acting oscillator
and an old engine was given a complete overhaul including an 'O' ring on
the piston and in the gland. Shaft bearings were drilled out and
long phosphor bronze bushes fitted at each end with a fair sized oil reservoir
between, whilst the old crankshaft was replaced by a new heavy disc crank
extending back over the front bush and with oversized, hardened, shaft
and pin pressed in.
Further wear at the gland neck was prevented by fitting a crosshead
guide bar to rock the cylinder, driven by a bush soldered to the, new,
big-end. Ports were opened out to the maximum permissible size (just
under 1/16") and a new 1/8" trunnion pin fitted; a small displacement lubricator
finished the job and the engine was run on the bench.
Although plenty of power was now available, heavy slogging at 30 psi
began to wear the soft brass trunnion bearing and allow the piston rod
thrust to separate the port faces. So a longer phosphor bronze bush
was fitted, together with a hardened pin and a labyrinth groove turned
in the port face.
Unfortunately even this only alleviated the problem and
under heavy load the port face still bubbled slightly. Although steam loss
was now infinitesimal and the wetness would have been unnoticed in normal
use, it was considered unacceptable in a balsa hull and the outboard trunnion
bearing shown in the photo was fitted. Pins and port face were lightly
skimmed with the cylinder assembly running between centres and the centre
in the outboard pin used to locate the steel ball which the leaf spring
on the outer bearing bears on.
Performance was now 100%. There was no trace of
leakage at 40 psi, whilst at only 10 psi it would turn a Stuart 2" x 5"
propeller at 750 rpm.
Attention now turned to the boiler and the twin drum design was
adopted, again because of height restrictions and after some experimenting
with steam drums and perforated pipes the curved connecting pipe was found
to give the driest steam.
It worked well and the boiler could be filled almost to
the top without priming, even in a 'rough sea'. The one bad design
feature is the 'remote' safety valve - this should have been fitted, horizontally,
to the side of the curved pipe.
The boiler was filled by an external hand pump, the high
level check valve backed up, via a syphon, by the car tyre valve mounted
on the base plate as a convenient, and dribble proof, coupling for the
connector..
To provide heat insulation the firebox is double skinned;
the two tinplate skins are approx 1/8" apart and the air supply to the
lamp is drawn down between them. This was very effective, the top
remained cool while at the hottest place, near the bottom, the temperature
never went above 110 degs/F until just after shut-down when it rose to
about 150 degs/F.
Two stoke hold ventilators and the gap between the funnel
and its liner provided all the air required and this allowed the superstructure
to be sealed to the deck, providing a very sea-worthy ship.
Draught is provided by the engine exhaust via an oil separator;
the steam entering this via a tangential pipe and leaving through a perforated
pipe in the centre. Without this draught the lamp suffocates almost
immediately to provide the necessary fail-safe. (and also make lighting
up a rather elaborate ritual - see later)
Early experiments with spirit lamps had shown that circular
wicks were only effective if diameter was limited to about 1/4", above
that size, the fuel evaporating from the centre didn't get sufficient air
to burn properly.
So long wicks were used, with air supply arrangements
based on those of a paraffin lamp but without a secondary supply.
These are divided approx' 1/3 from one end to provide
'full' and 'half' speeds and are fed from a standard 'chicken feeder' arrangement
operating at two levels, controlled by a lever operated by the four station
clockwork radio escapement. (which also provided Port or Starboard helm
in the intermediate positions) A balance pipe had to be connected
between the feed chamber and the firebox to equalize the pressures and
prevent the depression drawing neat fuel from the wicks, whilst cold air
leaking into the box alongside the fuel pipes, prevented vapour locks.
One rather strange feature was the effect of engine speed
on steam raising. Allowing the engine to race, greatly increased
the draught to both evaporate more spirit and provide the air required
to burn it. I had certainly not expected to get involved in 'grate
loading'.
The rather complicated starting procedure was also vaguely
reminiscent of loco practice - to the total bewilderment of the other pond-siders.
A plug cock, situated against the back head where it could be operated
by a rod connected to a concealed lever on the superstructure, was connected
to 'short-circuit' the engine and connect the steam pipe directly to the
oil separator via a 1/32" hole. This was the 'blower' valve.
Starting with the boiler empty and the whole unit removed from the hull
to give access to the lamp lighting door, this cock was opened and a rubber
tube with a bulb was attached to the separator drain valve. The lamps
were lit and the bulb was used to pump air up the blast pipe, drawing sufficient
air past the wicks to keep them burning after the lighting door was closed.
In a very short time the water tubes were hot and a single pumpful of water
was fed into the boiler. This burst into steam immediately it reached
the tubes and after a few seconds warming up the plumbing, it reached the
blast pipe. The separator drain was now closed, the rubber tube removed,
and, with the engine ticking over gently on the pressure drop across the
1/32" hole, the boiler very carefully pumped to the level of the
try cock. The fuel tank could now be topped up, the separator drained
and the whole unit wiped clean before the engine was stalled on a dead
centre and it was fitted into the boat. With the superstructure fitted
and the boat in the water the engine was started again before closing the
blower and, after a quick check of the radio control, away she went ----
With Bluebell in the water several propellors were tried before arriving at that strange four bladed, flat tipped, 2.5"x4.5" 'heavy duty wheel' cribbed from a very old American 'Mechanic's Guide'. This was the most satisfactory by far, the boat riding as steady as a rock with 15 ozs in the tow rope when pulling my two boys in a heavy canoe at just over 1 mph. (scale 7 knots)
Now we come to the really sad part :-(
Many early morning runs were made, with the plant's performance
100% reliable and consistent - and this was to prove my undoing - I got
bored and measured its performance. 65ccs of spirit
was sufficient to raise steam and then run the engine at full power for
20-23 mins, a total work output, at the tow hook, of 1800 ft/lbs, giving
an overall efficiency of 0.18%. A whole order of magnitude behind
IMLEC and a challenge.
I decided to modify the engine for expansive working and
spent several happy weeks designing and making a stainless steel plate
valve fitting between the port face and the cylinder, and oscillated by
an eccentric machined on the flywheel.
This was an unmitigated disaster. Not only did it
leak steam but the engine would only run at high pressure and speed.
Much time was spent on modifications and I did succeed
in reducing leakage to a dribble - but the engine was still very inflexible
and I was considering making new port faces and returning to non-expansive
working when I noticed the damaged hull. Several pond side knocks
had allowed the balsa to get damp, this had broken the cement joints and
things were coming apart at the seams!
I gave up - wrote up the whole unhappy affaire in M.E.
(21-5-76) and forgot poor Bluebell -----
Propellor
test (superstructure not fitted) - pond stirring at 1 MPH!
Too clever by half! - The plate-valve oscillator would only run at high speed and within a narrow pressure range.